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西北某铁路风积粉细砂路基填料改良试验研究
Experimental Study on Improvement of Filling Material for Aeolian Silt Roadbed of a Railway in Northwest China

DOI: 10.12677/HJCE.2021.101008, PP. 67-74

Keywords: 铁路路基,填料改良,室内试验,现场试验,对比分析
Railway Subgrade
, Filling Improvement, Indoor Test, Field Test, Comparative Analysis

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Abstract:

根据西北某铁路路基填料压实困难,制定改良方案。通过室内进行含水率试验、击实试验、无侧限抗压强度试验试验,结合试验结果在现场做试验段,对风积粉细砂路段路基填料改良前后的性质分析对比。研究表明,现场试验段碾压后测定的改良后各项指标较改良前有所提升。该研究成果对西北其他地区铁路风积粉细砂路基填料改良具有一定指导意义。
According to the difficulty of filling compaction of a railway subgrade in the northwest, an improvement plan was developed. Through indoor water content test, boundary water content test, compaction test, unconfined compressive strength test, combined with the test results in the field test section, the properties of the aeolian silt fine sand road subgrade filling before and after improvement were analyzed and compared. Studies have shown that the improved indicators measured after rolling in the field test section have improved compared with those before the improvement. The research results have certain guiding significance for the improvement of railway aeolian silt subgrade filling in other areas in the northwest.

References

[1]  张洋, 张艳召, 吴广陵, 等. 风积沙压实特性及填筑重载铁路路基压实工艺[J]. 铁道建筑, 2017(3): 77-80.
[2]  任辉明, 曾新迪, 师高鹏等. 水泥改良风积沙无侧限抗压强度试验研究[J]. 兰州交通大学学报, 2017, 36(4): 67-72.
[3]  袁玉卿, 王选仓. 风积沙压实特性试验研究[J]. 岩土工程学报, 2007, 29(3): 360-365.
[4]  陈忠达, 李万鹏. 风积沙振动参数及振动压实机理[J]. 长安大学学报(自然科学版), 2007, 27(1): 1-6.
[5]  中华人民共和国铁道部. 铁路工程土工试验规程: TB 10102-2010 [S]. 北京:中国铁道出版社, 2011.
[6]  国家铁路局. 铁路路基设计规范: TB 10001-2016 [S]. 北京:中国铁道出版社, 2017.

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