%0 Journal Article %T 天然气井油管悬挂器腐蚀失效分析 %A 刘守平 %A 周上祺 %A 王佳眉 %A 任勤 %J 腐蚀科学与防护技术 %P 253-255 %D 2004 %X 用金相显微镜、扫描电镜、X射线衍射仪和X射线能谱仪对天然气井油管悬挂器腐蚀失效进行了检测分析,并对天然气井油管悬挂器用35CrMo钢进行了盐雾试验,结果表明,天然气中的水和CO2是引起腐蚀的主要介质,腐蚀产物主要是FeCO3,高速天然气冲刷和钢中的非金属夹杂加剧了腐蚀的速度.CORROSIONFAILUREANALYSISOFANOILTUBEUSEDINNATURALGASWELLLIUShou-ping,ZHOUShang-qi,WANGJia-mei,RENQinChongqingUniversityAfailedoiltubeusedinnaturalgaswellwasexaminedbyopticalmicroscope,scanningelectronmicroscope,X-raydiffractometerandX-rayspectrometer.Corrosionbehaviorof35CrMosteelsamplesoftheoiltubewereinvestigatedbymeansofsaltspraytestsinthelaboratory.TheresultsshowthatCO2andH2Oareprimaryfactorsinthecorrosionofoiltube.ThecorrosionproductisFeCO3,non-metallicinclusionsinthesteelanderosionofnaturalgasfluidplayedanimportantroleinacceleratingthecorrosion.oiltube;naturalgaswell;35CrMosteel;failureanalysis;corrosion %K 悬挂器 %K 35CrMo钢 %K 失效分析 %K  %U http://www.cspt.org.cn/CN/abstract/abstract287.shtml